IMPLEMENTASI METODE QCC UNTUK PENGUKURAN REJECT SIZE PARTIAL SQUEGEE MESIN KTL-1 PADA PROSES PRODUKSI BAN

PAMBUDI, MUHAMAD RESTU AWAL (2024) IMPLEMENTASI METODE QCC UNTUK PENGUKURAN REJECT SIZE PARTIAL SQUEGEE MESIN KTL-1 PADA PROSES PRODUKSI BAN. S1 thesis, Universitas Mercu Buana Jakarta.

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Abstract

This research was conducted in the tire manufacturing industry, this research discusses a case study of improving the quality of Partial Tubeless Squegee, by identifying Partial Tubeless Squegee defects in the process of making Tubeless Size Partial Squegee. The total defects in the KTL-1 Machine in the period January 2023-April 2023 amounted to 7,174,881 m from the total production amount of 7,712,621 m. From this amount, the defect percentage was obtained at 93%, which exceeded the company's defect tolerance limit, namely 5%. Field observations and collection of production data and product defect data as data collection methods. Based on the research results, by implementing the QCC (Quality Control Circle) method, the types of defects in Tubless Squegee Partial can be identified. Then the factors causing the Tubeless Squegee Partial problem can be identified, namely the roll press surface is uneven due to wear out by friction, the bearing is not lubricated properly, and the cylinder seat is not flat. So that the results of this analysis can provide suggestions for improvements to the Tubeless Squegee Partial defect problem. From the results of improvements that have been carried out using the QCC (Quality Control Circle) method, namely repairing uneven cylinder seats and repairing the surface of the roll press which has been wore out due to friction. Implementation of corrective actions succeeded in reducing the Tubeless Partial Squegee Reject Rate from 92% to 7%. Penelitian ini dilakukan di industri manufaktur produsen ban, penelitian ini membahas studi kasus perbaikan kualitas Tubeless Squegee Partial, dengan mengidentifikasi defect Tubeless Squegee Partial pada proses pembuatan Tubeless Size Partial Squegee. Total defect di Mesin KTL-1 pada periode Januari 2023-April 2023 sebesar 7.174.881 m dari total jumlah produksi yaitu sebesar 7.712.621 m. Dari jumlah tersebut didapatkan persentase defect sebesar 93% yang melewati batas toleransi defect perusahaan yaitu sebesar 5%. Observasi lapangan dan pengumpulan data hasil produksi serta data defect produk sebagai metode pengumpulan data. Berdasarkan hasil penelitian, dengan implementasi Metode QCC (Quality Control Circle) jenis defect pada Tubless Squegee Partial dapat teridentifikasi. Kemudian faktor-faktor penyebab masalah Tubeless Squegee Partial dapat teridentifikasi, yaitu permukaan roll press tidak rata karena terkikis gesekan, bearing tidak terlumasi dengan baik, serta dudukan silinder tidak rata. Sehingga dari hasil analisis tersebut dapat memberikan usulan perbaikan dari masalah defect Tubeless Squegee Partial. Dari hasil perbaikan yang sudah dijalankan menggunakan Metode QCC (Quality Control Circle), yaitu memperbaiki dudukan silinder yang tidak rata dan memperbaiki permukaan roll press yang terkikis akibat gesekan. Implementasi tindakan perbaikan berhasil menurunkan Reject Rate Tubeless Partial Squegee dari 92% menjadi 7%.

Item Type: Thesis (S1)
Call Number CD: FT/IND. 24 073
NIM/NIDN Creators: 41622110032
Uncontrolled Keywords: Defect, Kualitas, QCC
Subjects: 600 Technology/Teknologi > 620 Engineering and Applied Operations/Ilmu Teknik dan operasi Terapan
700 Arts/Seni, Seni Rupa, Kesenian > 750 Painting and Paintings/Seni Lukis dan Lukisan > 758 Other Subjects/Subjel Lainnya > 758.6 Industrial and Technical Subjects/Subjek Industri dan Teknik
Divisions: Fakultas Teknik > Teknik Industri
Depositing User: ANANDA NADIRA PUTRI
Date Deposited: 20 Sep 2024 01:47
Last Modified: 20 Sep 2024 01:47
URI: http://repository.mercubuana.ac.id/id/eprint/91589

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