ERDIYANTO, ANTO (2020) PENERAPAN LEAN MANUFACTURING PADA PRODUKSI PIPE PILLION R/L ASSY DENGAN MENGGUNAKAN VALUE STREAM MAPPING. S1 thesis, Universitas Mercu Buana Jakarta.
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Abstract
Pipe pillion R. L ASSY is one part component that is located in the framework of the motorcycle manufactured by PT AAP. Based on performance report delivery, delivery part to customer always experienced delay due to not achieving the result of plainning production and high leadtimes number on the production floor. Pipe pillion R. L ASSY produced by 9 workstations that there are 69 activities in the production of 69 activity there is activity Value added of 37 activity and 32 activities non value added with the amount of cycle time of 435.54 seconds, travel distance of 261 meters and the number of lead time of 2.161 days. Therefore, it should immediately evaluate and repair the ongoing production process. The method used in this research is value stream mapping that is the scope of Lean manufacturing to see the flow of material and product information that runs from the raw material form to the final product until the customer's return where the problem occurs. The purpose of this research is to know the cause of the production process failure in achieving plainning. After analysis carried out with Kaizen Blitz Then there are 5 factors causing the failure to be repaired IE, activity on each workstation, workstation cutting Celculer part pipe pillion R step k81a, workstation cutting Celculer part pipe pillion l Step, workstation polishing and distance handling between workstations. Then the improvement efforts based on the Forum Group discussion (FGD) is with: improvement activity on each workstation activity (workstation blank pierching: Material placement rack of materials plate ribbon, bending workstation: shootermaking, worstation bending hamming: shootermaking, workstation marking: shootermaking, belts workstation : Material WIP shelf manufacturing), improvement Workstation cutting: Manufacture of dies Proggresif Profit cutting process in stamping machine, improvement Workstation polishing: Eliminating process activity polishing, improvement distance handling between workstations: Change of machine layout production, manufacture of rack dies in area Building 1 departement Press. After the improvement by using the value stream mapping where the number of cycle time to 79.82 seconds or down by 355.72 seconds, the number of leads time to be 0.202 or down by 1.959 days and the number of travel distance to 36 meters or down by 225 meters. Keyword: Pipe pillion R. L assy. Target plainning. Lead Time. Value Stream Mapping. Kaizen Blitz. Focus Group Discussion (FGD). Pipe pillion r.l assy merupakan salah satu komponen part yang berada pada bagian kerangka sepeda motor yang diproduksi oleh PT AAP. Berdasarkan performance report delivery, delivery part ke customer selalu mengalami keterlambatan yang dikarenakan tidak tercapainya hasil plainning produksi dan jumlah leadtime yang tinggi pada lantai produksinya. Pipe pillion r.l assy diproduksi oleh 9 workstation yang dimana terdapat 69 aktivitas dalam produksinya dari 69 aktivitas terdapat aktivitas value added sebesar 37 aktivitas dan 32 aktivitas non value added dengan jumlah cycle time sebesar 435,54 detik, travel distance sebesar 261 meter dan jumlah lead time sebesar 2,161 hari. Oleh karena itu harus segera melakukan evaluasi dan perbaikan terhadap proses produksi yang berlangsung. Metode yang digunakan dalam penelitian ini adalah value stream mapping yaitu ruang lingkup dari lean manufacturing untuk melihat aliran material dan informasi produk yang berjalan dari mulai dari bentuk raw material hingga produk final sampai ditangan pelanggan dimana terjadinya masalah. Tujuan penelitian ini adalah mengetahui penyebab kegagalan proses produksi dalam pencapaian target plainning. Setelah dilakukan analisis dengan kaizen blitz maka terdapat 5 faktor menyebabkan kegagalan yang harus diperbaiki yaitu, aktivitas pada setiap workstation, workstation cutting celculer part pipa pillion r step k81a, workstation cutting celculer part pipa pillion l step, workstation poles dan jarak handling antar workstation. Maka upaya perbaikan berdasarkan forum group discussion (FGD) adalah dengan: improvement activity pada setiap aktivitas workstation (Workstation blank pierching: pembuatan rak penempatan material plate pita, workstation bending: pembuatan shooter, worstation bending hamming: pembuatan shooter, workstation marking: pembuatan shooter, workstation assemblies: pembuatan rak wip material), improvement workstation cutting: pembuatan dies proggresif untung pemakaian proses cutting dimesin stamping, improvement workstation poles: menghilangkan aktivitas proses poles, improvement jarak handling antar workstation: perubahan layout mesin produksi, pembuatan rak dies diarea gedung 1 departement press. Setelah dilakukannya improvement dengan menggunakan value stream mapping dimana jumlah cycle time menjadi 79,82 detik atau turun sebesar 355,72 detik, jumlah lead time menjadi 0,202 atau turun sebesar 1,959 hari dan jumlah travel distance menjadi 36 meter atau turun sebesar 225 meter. Kata Kunci: Pipe Pillion R.L Assy. Target Plainning. Lead Time. Value Stream Mapping. Kaizen Blitz. Focus Group Discussion (FGD)
Item Type: | Thesis (S1) |
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Call Number CD: | FT/IND. 20 056 |
NIM/NIDN Creators: | 41615120075 |
Uncontrolled Keywords: | Pipe Pillion R.L Assy. Target Plainning. Lead Time. Value Stream Mapping. Kaizen Blitz. Focus Group Discussion (FGD) |
Subjects: | 600 Technology/Teknologi > 650 Management, Public Relations, Business and Auxiliary Service/Manajemen, Hubungan Masyarakat, Bisnis dan Ilmu yang Berkaitan > 658 General Management/Manajemen Umum > 658.5 Management of Production/Manajemen Produksi 600 Technology/Teknologi > 670 Manufacturing/Manufaktur, Pabrik-pabrik 700 Arts/Seni, Seni Rupa, Kesenian > 750 Painting and Paintings/Seni Lukis dan Lukisan > 758 Other Subjects/Subjel Lainnya > 758.6 Industrial and Technical Subjects/Subjek Industri dan Teknik |
Divisions: | Fakultas Teknik > Teknik Industri |
Depositing User: | Dede Muksin Lubis |
Date Deposited: | 07 Mar 2022 16:25 |
Last Modified: | 21 Feb 2023 02:36 |
URI: | http://repository.mercubuana.ac.id/id/eprint/57386 |
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